Saturday, August 26, 2017

Fit so nice, I made it twice....

Actually, it was the wrong material, so I kicked myself a few times and bought a new flywheel. This time, a *forged* flywheel, not a *cast* flywheel. Had I the sense to do more research ahead of time, I'd have only made it once. Nonetheless, the new version is around 300% *less* likely to break apart during flight.

That's version 2. Same dimensions, but machines a lot more like 4130 than the first one.

In this blurry picture I'm pointing out the locating step for the flexplate. That way I know it's concentric. I did the same on the inside for the prop extension:

Now that this is finished, I was able to start test assembling the crankcase. First, the connecting rods on the crankshaft:

Drop the crank assembly into the case and add some nuts, torqued to spec:

It still rotated freely after it was torqued, so that was a good sign. No rubbing or clearance issues so far. The next step was to add the head studs and check the piston deck height. I painted my head studs to help avoid corrosion:

And then I added them to the pile.

I added a cylinder and piston, and started taking measurements. I used a .030" shim under the cylinder, which is how the engine came to me. I set up my dial indicator and rotated the crank to TDC for that cylinder.

Zero'd up the dial indicator (though the photo makes it look off);

Using a piece of steel rod I had laying around as a straightedge, I measure deck clearance + rod width at 0.428" or so.

The rod I used measured 0.314", which means my clearance distance is 0.114". That's a lot more than I want! VW specs are between 0.040" and 0.080". I went back and checked, and the old pistons are the same as the new ones, and the old cylinders were within a couple thousandths of the new ones. That means that this engine was assembled wildly out of spec.... which shouldn't be a surprise, but it was. And means more work; removing the shims brings me down to 0.084", which is out of spec (and 0.024" more than I really want.) That means I'll have to chuck each cylinder up on the lathe and turn it down to what I want. 


...unless the heads are also anomalies, and have a much smaller chamber than normal heads, in which case the cylinders need to be extra long.... Bottom line, the new priority is get the heads reconditioned and blueprinted so I know what kind of setup I need.

There has been nothing straightforward about this engine. Armed with the knowledge I've gained from this process, I believe the next engine I assemble will be from brand new parts that I know the details on.

Monday, August 7, 2017

...And flywheel solutions!

I removed all the dowel pins from the crankshaft, which wasn't super difficult this time around... I think my holes are a light press fit, rather than the super-tight holes that were there originally. I'm not sure if that'll cause problems down the road or not; they are still a press fit, so load should (theoretically?) be transferred just as effectively.

The flywheel face on the crankshaft seemed to have zero runout when sitting in the crankcase, but there were a few problems with how I was taking that measurement that could have absorbed imperfections... so I decided to throw it at the lathe and check runout by painting the face with red dykem and scraping a tool along the face. The goal was to avoid removing any material, just rub the dykem off, and see if it was a gnarly edge on a dowel hole that was causing issues, or if the face itself was not perpendicular to the axis of rotation. I thought I took a picture of the result, but apparently this was another instance where my phone shut off instead of taking a picture... that's been happening a lot recently.

Anyways, the dykem was scraped off of about half the face, and the other half the dykem was still there; it made almost a perfect half circle of red and a half circle of steel. Now, the crankshaft was out about .0005 on each end, and I failed to document whether it was out the same direction at the same point in rotation; so when I did the math, I had to assume worst-case of the crankshaft being out a full thousandth of an inch. Even so, the pattern was much too extreme to blame it on a misalignment of that magnitude, so I turned a couple thousandths off the entire face. When I re-attached the flywheel, it was only out about 1 thousandth of an inch as opposed to the 8 I had before, so I put the dowels back in and put the flywheel back on. I put the whole thing on the lathe as an assembly, because I have to do a little more work on the flywheel.

Now to the part I have pictures of! The final flywheel is going to be two parts riveted together. The inside part will be turned from the original flywheel, and the outside is from a much lighter flexplate (which basically just positions the ring gear and transfers the load from the starter.) I cut the inside out of the flexplate on a CNC mill at work, since it was too big to turn on the lathe.

I also cut the outside off of the flywheel on the mill, but left it oversize so I could finish it on the lathe.

I could have programmed the mill to cut a circle, but I wanted to use a rotary table to get a true circle on the flexplate, since I can't touch that up on the lathe. Once I was set up to do that, it was just easier to do the same with the flywheel.

Once the flywheel and crankshaft assembly were on the lathe together, I started working towards the final shape. There's a step on the outside of the flywheel that needed to be turned flat with the rest of the face, and then a new step needed to be cut out from 5" diameter outwards to accept the flexplate. I've got the whole thing turned flat, and I used some red dykem to help me visualize where that 5" diameter will be.

It's been a little tough to find time to work on this stuff, but I think I see the light at the end of the tunnel. I have a few more parts on order, and once they get here I should be able to begin the reassembly process... which should be a pretty quick process, given how much documenting and adjusting and tweaking I've done *before* started to put it all together.

Saturday, July 15, 2017

Lathes + Flywheel Troubles

Having a metal lathe, even a small one, is a fantastic way to avoid paying a large amount of money for a small amount of work. I started by chucking up the crankshaft and adjusting until I had less than a thou of runout. That's still too much for bearing work, but I'm not doing bearing work. I put a 45º chamfer on the flywheel mating face, and knocked the burrs off of the pulley hub mating portion of the shaft. A little polishing to make sure the pulley hub slips on, and we're off to the races. The pulley hub was heated to ~400º F, the crank cooled to ~10º F. I still had to use some persuasion with a hammer to seat it fully, but she's on there now.

The two aluminum rings are the replacement seal housing, complete with seal installed. I must've walked through the assembly process a dozen times to make sure I put the seal housing on the correct way, and I still checked it half a dozen times afterwards. The red material is a cut up silicon baking sheet to help keep the rubber on the seal from melting/losing its elasticity.

After I turned the chamfer on the flywheel end, I re-installed the 4 dowel pins. The bottom pin in the picture is larger than the rest, allowing me to index the flywheel. My plan is to mark TDC on the flywheel, since it can only line up one way, and with very tight tolerances.

When I attach the flywheel and snug up the nut, I still end up with about .008" of runout at the edge of the flywheel. Not a lot, but more than I'm willing to put this together with. I used some more PlastiGage between the flywheel and the crank surface to make sure I was fully seating the flywheel... sure enough, I wasn't, and the place where I wasn't touching the crankshaft is the same angle where the flywheel is furthest out. There are four factors at play here; the crankshaft face, the dowel pins, the flywheel face, and the flywheel holes for the dowels. The crankshaft face is most likely true, since that's how it was run successfully before, and my PlastiGage test seems to confirm it. I proved that the flywheel face was true by using a rotary table and a dial indicator and getting less than a thousandth of runout. I think that leaves the dowels. How did that happen?

It happened pretty simply - I used the flywheel to drill the dowel holes. Normally, this would've been the best way to go about it. However, because of that radius on the flywheel that I chamfered the crank to match, the flywheel wasn't sitting quite right on the crankshaft, which means the dowels are *slightly* cocked to one side, which means they *want* to pull the flywheel that way.

So my next step is to torque the flywheel to spec, which is some ridiculous number above 200 ft/lbs, and see if that fixes the problem. If not, I may have to get creative. On a positive note, the only bit of clearancing that I still need to do involves grinding a little material off one of the connecting rods. Once that's complete, I can start setting things out for assembly. I do, however, need to get this flywheel thing straightened out before I can move forward.

Monday, July 3, 2017

Dowels are hard, PlastiGauge is soft.

It took a lot of work, but I got all four dowel pins out without damaging the crank. The two I put in came out easily enough with some vise grips and a bit of twisting and pulling... the two that were in from before were another story entirely. Nothing would touch them, including the hardened jaws of a *nice* set of vise grips. (Those are no longer a nice set of vise grips, by the way.) In the end, I discovered why machinists have drill bit sets up to half an inch with just a couple thou of difference all the way up...

...It's because hardened steel pins can't be drilled out with big steps between bit sizes! It took me a solid hour and a half to drill each pin out. However, both of them twisted out right before I broke through the wall of the pin (after a couple good taps with a hammer on the side of the pin to break it up a bit.)

I checked the face on a dial indicator, and at most it's out a single thousandth at the edge. That's about an inch from center, which means that might account for about 5 thousandths at the edge of the flywheel.... which means something else is amiss. I checked the flywheel by placing it on an indexer, supported by placing a tight tolerance block between the indexer and the mating face on the flywheel. Spin the indexer, check for runout.... I forget what I got, but it was insignificant (which is why I forgot it. :D) I was pretty puzzled at that point. However, since the pins were out of the crank, I was able to rotate the flywheel on the crank. How does that help us? Well, before I pulled the dowels, I'd marked on the flywheel exactly *where* the runout was, as well as *how much.* When I put the flywheel back on after the pins were out, I lined it up pretty close to where it was originally... and got pretty much the same results. (I didn't use an indicator, as I was less interested in how much it was out as *where* it was out.... and it was wobbling pretty obviously.) Ok, repeatability, that's good. So I rotated the flywheel 180 degrees and tried again. If it was the flywheel, that should've made no difference; the marks on the flywheel still should have been correct. If it was the crank face that was out, then the marks on the flywheel should have been exactly (or close to) opposite what the flywheel was showing the second time around.

So what did I find? Well.... actually, it was about 70 degrees off from where it was originally. I didn't know what to make of that, until I started taking careful measurements of everything. What I found was that the flywheel had a bit of a radius where it mated with the crankshaft, and the crankshaft did not have that radius. I think what's happening is that there's a tiny bit of play between the *side walls* of the flywheel and the crankshaft, and the radius causes the face of the flywheel to be tighter than the crankshaft can fit into. Add the radius and a little bit of slop and, unless the radius on the flywheel and the edge on the crankshaft are perfectly uniform and smooth, odds are the flywheel just isn't seating fully and is staying at a bit of an angle. The fix is simple; just cut a matching radius (or, much easier, a slightly relieved chamfer) on the crankshaft. The side walls and dowel pins will still locate the flywheel, and the face where the two meet won't lose much area. I like that idea better than cutting a sharp corner into the flywheel. 

I should mention, the reason that this is an easy fix is because I recently picked up a Jet 9x20 metal lathe. Just as soon as I finish getting that set up in the basement, this will be a pretty straightforward job. I'll be spending my evenings this week cleaning it up and, as soon as my insert tooling shows up next week, I'll be making chips and breaking tools. Also touching up airplane engine parts. 

I also got my oil galley plugs straked in place so they can't rotate out. I found one of my case savers was loose, so I used some red LocTite, filed a notch in it, and straked that in place as well. 

The last thing I wanted to do today was check my connecting rod bearing clearance. If you've never heard of PlastiGauge, you're in good company; none of the auto parts stores I went to had ever heard of it either. I ended up at a local NAPA, a company I spent 6 years working as a counterman for, and gave the kid at the counter the part number I remembered as being correct. "Huh, it says we've got 12 in stock. What is it again?" It comes from the warehouse packaged as a dozen, so I guess it shouldn't surprise me he'd never heard of it; he'd never sold any of it. Anyways, PlastiGauge is a kind of plastic-y wax string that's very precisely formed. A strip of it is placed between two surfaces you want to check clearance on, and those two surfaces are brought together however they will be brought together during final assembly. In this case, those surfaces are the connecting rods with bearings installed, and the crankshaft. Blurry picture, but the green little stripe in the middle of the white grease is the PlastiGauge before the con rod is tightened....

...And after:

The lighting was pretty awful. However, I can tell you that the strip of green that's *not* a weird reflection is the one above the .0015" mark. Basically, that wax gets squished to different widths based on how much clearance is available, and the package the wax comes in has a gauge on the side to check it with. All four journals had *exactly* the same width as the .0015" mark, and they were all very even stripes from one side of the journal to the other. (If the journals or the con rods had any taper, that would've shown up as a tapered stripe.) The specs for this engine are 0.0008-0.0025, so I'm smack in the middle of where I want to be. Any wear is going to cause that clearance to open up, and I've got a solid thousandth of an inch for it to open up before I make it out of the range I want to be in.

I'll putz around with little things here and there, but mainly I'll be setting up that lathe and taking some test cuts to get to know it. I've got to do my touch up on the crankshaft, and a couple other things, and then I can start test assembling everything. 

Sunday, June 18, 2017

MORE Case and Crank prep...

It's been slow going lately, but progress seems to be taking place. I got lost in a lot of thought experiments and what-ifs, and (as is usually the case,) ended up right back where I started. So I cut the top off of the flywheel flange on the case, did a little bit of clearing on the inside of the case (some spots didn't seem to have more than a few thou of room for rotating parts), and used a Dremel to carve away a couple of channels for the engine mount in the back.

I also pulled all the aluminum plugs to get an idea of how much stuff was trapped in the case...

...And there was a lot! Much of that was from walnut blasting the case, but I found a good number of metal shavings as well. I'm glad I pulled the plugs... Next I tapped the holes for various pipe thread plugs, ranging from 1/16" NPT up to 3/8" NPT. I used a 1/2" NPT to tap a larger hole in the front for an oil temp sensor, because I've read bad things about the current temp sensor location (near the flywheel end of the case) actually reading quite a bit lower as a result of not being in a high-flow area. The new place is directly in the oil flow as it enters the oil pump, so it'd be hard to get a better reading than that!

Drilling and tapping the magnesium was quite easy, actually... in that the magnesium tapped without much force. There were a few places that I had to tap a few threads, then grind the tap down, then tap a few more, then grind, back and forth a few more times until the plug fit the way I wanted it to. There's one hole that I may have tapped just a little too hard and began to mess up the threads, but the plug threads in just fine and seems to have full contact along the entire length and circumference of the plug, so I'm going to leave it.

Now that all of the holes are prepped, I'll pull all the plugs out for another cleaning session. The last step will be to file a notch in each of the plugs so I can swage the case metal into those notches as a final insurance against the plugs working their way back out.

I forgot to take pictures, but I drilled the crankshaft for a couple more dowel pins. When I received it, it only had two, which was probably fine running the prop off the other end, but I'm not comfortable only using two running it with the prop hanging off the flywheel. So I drilled two more holes, reamed them, and tried to put the dowels in.... oops! One of the holes is *way* too loose! So I ordered a 11/32" drill bit blank, cut it down to the right length to be a dowel pin, and re-reamed the hole to be a press fit. This really isn't a bad plan anyway, as it keeps my flywheel aligned the same way every time it's reassembled, and the only extra work I'd have to do on a new flywheel is drill one hole slightly larger.

Upon reassembly of the flywheel and crank, I realized the flywheel is running about 60 thousandths out of true at the outermost edge. Not cool at all. So my next step is to remove the dowels and see if the crank face is out, but my bet is that somewhere along the way some burrs crept up and are keeping the crank from seating correctly. At least, I hope that's what happened... otherwise it's back to the machine shop.

Monday, April 10, 2017

Starting to prep for assembly.... sort of.

With my crankshaft back and polished, I was able to begin reassembling the gears onto the nose.  First the key:

Heat up the cam drive gear, and slip it on:

Next the spacer and the new brass distributor gear.

I'm working out the best way to attach the prop hub - I know what orientation, but if I want it repeatable to exactly the same spot, I'll need to build some kind of jig that locates off of the cam drive gear. I'm not sure how much that will matter at this point.

In the meantime, I finished walnut blasting the case, and decided to try it on the heads as well. They were somewhat improved, but I'll still try soaking them in carb cleaner to try and get rid of more of the carbon that's built up. Ignore the ape blocking part of the picture...

And below, a chamber in progress to show my future self that it was, in fact, having an effect:

Once everything was sufficiently blasted, I used Simple Green to clean the case as best I could. I'll admit, I focused a little more on the outside than the inside, but I think it's pretty clean all the way through.

Once clean and dry, I cleaned the outside with solvent and got ready to paint. Bob Hoover says three things about painting the case: Do it, do it black, and do it thin. When I got the case, it was painted a dark gray... over top of a dark blue. Two layers of paint, the outer one fairly thick, were definitely not going to help much with thermal transfer, and yet it still flew that way. In light of that fact, I took Bob Hoover's advice on two of the points: I painted it, and I painted it thin.... and I painted it red.

I figure the color is less important than the paint thickness, so I cut the paint with Naptha and brushed it on, making sure to run the brush over any areas that looked like they had extra paint. The end result is definitely brush-textured, and not exactly what I had envisioned, but it looks pretty nifty all the same... and more importantly, it's protected from corrosion and it's not likely to overheat from the paint. I'll put this in the oven like I did the cylinders to get the paint nice and hard... it makes a big difference!

Friday, March 31, 2017

Good news! (And also, electronics are finicky!)

Just a quick pseudo-celebratory post - all of the work I've been doing on this engine has been under the shadow of uncertainty. The engine was involved in an off-airport landing, and I've been wondering if my crankshaft had sustained any damage. If it had, this engine would probably be scrap, based on how it had been modified - the major modified parts just don't seem to be readily available, and other manufacturer's modified parts wouldn't fit, and that would mean I'd need a new crankshaft, prop hub, and engine case, and they'd all have to be machined... Got it back from the machine shop today with a clean bill of health. Now I just have to finish cleaning and painting a few things, and the reassembly can begin.

In other news, apparently circuit design is a little tougher than I thought... received the PCB I had printed for my landing lights, (they look FANTASTIC, by the way - really like the purple solder mask with the gold solder pads) soldered everything in place, and... nothing. Back to the drawing board...